actfate 发表于 2012-6-2 15:22:14

求助四机两区域动态仿真

潮流结果和PSASP的完全对得上,但在不设故障情况下在0.17s失稳,G1的Pelec如图


lofl
ACTIVITY RTRN TO RETURN TO DYNAMICS--ACTIVITY?
Executing activity read,file
read,file
ENTER INPUT FILE NAME (0 TO EXIT, 1 FOR TERMINAL): 4g2a
ENTER IC, SBASE
ENTER TWO LINE HEADING
ENTER BUS DATA
ENTER LOAD DATA
ENTER GENERATOR DATA
ENTER NON-TRANSFORMER BRANCH DATA
ENTER TRANSFORMER DATA
ENTER AREA INTERCHANGE DATA
ENTER TWO-TERMINAL DC LINE DATA
ENTER VSC DC LINE DATA
ENTER SWITCHED SHUNT DATA
ENTER TRANSFORMER IMPEDANCE CORRECTION DATA
ENTER MULTI-TERMINAL DC LINE DATA
ENTER MULTI-SECTION LINE DATA
ENTER ZONE NAME DATA
ENTER INTER-AREA TRANSFER DATA
ENTER OWNER NAME DATA
ENTER FACTS DEVICE DATA
ACTIVITY RTRN TO RETURN TO DYNAMICS--ACTIVITY?
Executing activity fnsl
fnsl
ORDERING NETWORK
DIAGONALS =   10OFF-DIAGONALS =      9MAX SIZE =   18
ENTER ITERATION NUMBER FOR VAR LIMITS
0 FOR IMMEDIATELY, -1 TO IGNORE COMPLETELY: 99
ITER       DELTAP      BUS         DELTAQ      BUS      DELTA/V/      BUS       DELTAANG      BUS
   0      21.2968(      401   )    2.7013(      801   )    0.12761(      801   )   0.58266(      801   )
   1         4.2106(      801   )    8.1793(      901   )    0.12606(      701   )   0.04352(      1   )
   2         0.2518(      901   )    0.7799(      901   )    0.02045(      701   )   0.00508(      1   )
   3         0.0122(      901   )    0.0124(      901   )    0.00048(      701   )   0.00029(      801   )
   4         0.0000(      801   )    0.0000(      901   )    0.00000(      801   )   0.00000(      801   )
   5         0.0000(      801   )    0.0000(      801   )
REACHED TOLERANCE IN   5 ITERATIONS
LARGEST MISMATCH:    0.00 MW    0.00 MVAR   0.00 MVA AT BUS    801
SYSTEM TOTAL ABSOLUTE MISMATCH:               0.00 MVA
SWING BUS SUMMARY:
   BUS# X-- NAME --X BASKV      PGEN   PMAX    PMIN      QGEN   QMAX    QMIN
    301 4         20.000   700.1   9999.0 -9999.0   202.3   9999.0 -9999.0
ACTIVITY RTRN TO RETURN TO DYNAMICS--ACTIVITY?
Executing activity save,4g2a00
save,4g2a00
CASE SAVED IN FILE 4g2a00.sav ON SAT, JUN 02 201215:06
ACTIVITY RTRN TO RETURN TO DYNAMICS--ACTIVITY?
Executing activity cong
cong
GENERATOR CONVERSION COMPLETED
ACTIVITY RTRN TO RETURN TO DYNAMICS--ACTIVITY?
Executing activity conl all
conl all
ENTER % CONSTANT I, % CONSTANT G FOR ACTIVE POWER:
ENTER % CONSTANT I, % CONSTANT B FOR REACTIVE POWER:
LOAD TO BE REPRESENTED AS:
    ACTIVEREACTIVE
   100.00%   100.00% CONSTANT POWER
   0.00%   0.00% CONSTANT CURRENT
   0.00%   0.00% CONSTANT ADMITTANCE
ENTER 1 IF O.K., 0 OTHERWISE: 1
      2 OF      2 LOADS CONVERTED
ACTIVITY RTRN TO RETURN TO DYNAMICS--ACTIVITY?
Executing activity fact
fact
ORDERING NETWORK
DIAGONALS =   11OFF-DIAGONALS =   10MAX SIZE =   20
   11 DIAGONAL AND   10 OFF-DIAGONAL ELEMENTS
ACTIVITY RTRN TO RETURN TO DYNAMICS--ACTIVITY?
Executing activity tysl
tysl
ITER DELTAV/TOL X-------- AT BUS ---------XREAL(DELTAV)IMAG(DELTAV)
    1   0.003       1     0.3029E-07   -0.1089E-07
REACHED TOLERANCE IN   1 ITERATIONS
LARGEST MISMATCH:    0.00 MW    0.00 MVAR   0.00 MVA AT BUS    601
SYSTEM TOTAL ABSOLUTE MISMATCH:               0.00 MVA
ACTIVITY RTRN TO RETURN TO DYNAMICS--ACTIVITY?
Executing activity save,4g2a00
save,4g2a00
CASE SAVED IN FILE 4g2a00.sav ON SAT, JUN 02 201215:07
ACTIVITY RTRN TO RETURN TO DYNAMICS--ACTIVITY?
Executing activity RTRN
RTRN
ACTIVITY?
Executing activity DYRE
OUT OF FILE DATA--SWITCH TO TERMINAL INPUT MODE
GENERATOR MODELS USE:
CONS      1-    56
STATES      1-    24

SUMMARY OF MODELS READ:
GENS:GENROU
         4
NEXT AVAILABLE ADDRESSES ARE:
    CONSTATE    VAR   ICON
   57   25      1      1
NO MODEL CALLS IN CONNECTION ROUTINES--DYNAMICS SKELETON MAY BE USED
Executing activity CHAN

      3 OUTPUT CHANNELS HAVE BEEN ADDED
NEXT AVAILABLE ADDRESSES ARE:
   CHANNEL   VAR   ICON
      4      2      2
Executing activity STRT
GENROU AT BUS      1 MACHINE 1 : X'' =0.25000 IM(ZSORCE) =1.00000
GENROU AT BUS    101 MACHINE 1 : X'' =0.25000 IM(ZSORCE) =1.00000
GENROU AT BUS    201 MACHINE 1 : X'' =0.25000 IM(ZSORCE) =1.00000
GENROU AT BUS    301 MACHINE 1 : X'' =0.25000 IM(ZSORCE) =1.00000
   PTI INTERACTIVE POWER SYSTEM SIMULATOR--PSS/E      SAT, JUN 02 201215:08
1
2
INITIAL CONDITION LOAD FLOW USED1 ITERATIONS
----------------------------- MACHINE INITIAL CONDITIONS -----------------------------
   BUS# X-- NAME --X BASKV IDETERM   EFD    POWER    VARS   P.F.ANGLE   ID   IQ
      1 1         20.000 11.0300 2.4652700.00185.25 0.966770.87 0.7104 0.3249
    101 2         20.000 11.0100 2.5768700.00234.84 0.948159.45 0.7504 0.3109
    201 3         20.000 11.0300 2.4910719.00176.22 0.971344.98 0.7270 0.3303
    301 4         20.000 11.0100 2.5189700.10202.33 0.960733.50 0.7359 0.3181
INITIAL CONDITIONS CHECK O.K.
SNAPSHOT STORED IN FILE D:\PSSE30\EXAMPLE\4g2a.snp AT TIME =-0.020
CHANNEL OUTPUT FILE IS D:\PSSE30\EXAMPLE\4g2a.out
NETWORK NOT CONVERGED AT TIME =0.1700
26   191.996    801    0.1697E-01   0.8974E-02
Decimal number outside allowable range!
CHANNEL OUTPUT FILE IS D:\PSSE30\EXAMPLE\4g2a.out


潮流数据预处理应该没问题,dyr文件只包括发电机模型,用PSASP6型模型仿真结果正常,到PSS/E就出问题了

最后两项饱和度是自己随便写的,其他数据来自kunder的书

apsal 发表于 2012-6-7 01:07:16

问题很明显,你在执行STRT初始化操作时提示:
Executing activity STRT
GENROU AT BUS      1 MACHINE 1 : X'' =0.25000 IM(ZSORCE) =1.00000
GENROU AT BUS    101 MACHINE 1 : X'' =0.25000 IM(ZSORCE) =1.00000
GENROU AT BUS    201 MACHINE 1 : X'' =0.25000 IM(ZSORCE) =1.00000
GENROU AT BUS    301 MACHINE 1 : X'' =0.25000 IM(ZSORCE) =1.00000

这表明,你在潮流数据中的ZSORCE(CONG操作中将发电机等效为Norton电流源就是用的这个ZSORCE)与动态仿真中的发电机的次暂态电抗X"不相等。两个不相等,仿真就是错的。
这就是问题的所在。
看起来你的X"可能是对的,ZSORCE用的的默认值1.0,那么将潮流数据中发电机的ZSORCE的电抗值改为对应X"就可以了。

actfate 发表于 2012-6-7 12:46:15

厉害!!!光看INITIAL CONDITIONS CHECK O.K.去了
多谢::handshake::

mingyu 发表于 2012-6-7 14:54:02

学习一下。

wlm_28 发表于 2012-6-7 15:17:33

看不懂呀

lxself 发表于 2018-3-29 20:39:13

强啊强啊强啊强啊强啊

DUTshen 发表于 2019-8-14 20:35:29

谢谢!谢谢!谢谢!

BPA_CN 发表于 2019-8-14 20:44:44

同问,哪位大神指教一下?
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